Pi Wars Progress 16 Feb

Pi Wars Progress 

(16/2/2020)

We are getting ever so close to perfecting our design.Today we were messing around with the i2c motor driver again for our backup bot.We fixed up the code and flaws as well as assemble the backup bot.We managed to troubleshoot all the errors such as the robot not being able to turn 

This is the main code loop. 
It just controls the motors when the keys on the keyboard are pressed


This is the backup vehicle.We were assembling it.We had a problem with the wire coming off when the robot moved










Here's another look at the code.Of course this isn't final,we will improve the code and update again then

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